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The glass cylinders are already glued with "Sikaflex-292" silicone glue into the cylinder cover. One must be very careful to keep the glass surfaces ultra-clean. Even a fingerprint on the piston makes enough friction that it is hard to move inside the cylinder.
I have changed the flywheel quite a bit compared to the plan, where it was only a flat disk.
Assembly of the machineIt was a good feeling to put all these parts together.
Click on the pics to enlarge.
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Again a small change in the plans: for the connecting rods I used bush bearings out of brass (pic 22) instead of the 2 mm screws rotating directly inside the aluminum rods. I found that this had less friction and less radial clearance. These bushings are so tiny to hold that I made a simple vice for it (pic 23).
The slide gauge in pic 27 shows the clearance above the hot piston - 2 mm only between the piston top and the 'roof' of the heater!
The machine can only run with a sufficient temperature difference between the hot and cold cylinder. To maintain this I added a heat sink: for the prototype I used what I found in my cabinet: an aluminum sheet and two 2N3055 power transistors from the last century (pic 28), soon replaced by a fragment of an Intel 486 heatsink from my first computer (pic 29).
Runtime is approaching . . .Exciting moments when the blow torch heated the machine for the first time .... will she run? ..... yes, it took a lot of heat, but SHE DID RUN!
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Of course it was of interest how fast she was going. Pic 34 shows the bike speedometer that I borrowed from my Walking Beam machine. Initially it worked well - but the LSE-01 was too fast. After the machine exceeded 1600 rpm the instrument showed strange behaviour - probably the reed contact cannot change its status this fast. So what to do? Happily I remembered that I own a oscilloscope from my electronic days. I quickly grabbed a toothpick and 20 cm of varnished copper wire and twisted it around the toothpick's end. A magnet was taped to the flywheel, the coil positioned close to it - and I could read/calculate the speed: 1775 rpm. This not even close to the 3000 rpm that Koichi stated, but he is a master machinist, and this is an apprentice's work, my very first machined engine.
Possible reasons:
In any case, many thanks to Koichi
Hirata for this great plans which worked from the stand
for me.
As well, big thanks to Willi Bührer, a master
machinist in a neighbouring town, who helped me with materials
and straight tipps.
Finished during May 2007 by Ulrich Hornstein.

Copyright(c) 2007 by uh-lab.de